Electrical Isolation Incident

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Questions and Answers

An electrician re-installed fuses on a 930V DC electrical system believing the system was isolated. Which of the following factors contributed to this incident?

  • The electrician correctly followed the equipment Standard Operating Procedures (SOP).
  • The vessel was in port, minimizing the risk associated with energized work.
  • The electrician used a fuse insertion tool rated below the system voltage.
  • There was no Permit to Work (PTW) in place, and the cabinet was not properly secured or tagged. (correct)

During maintenance on a vessel, a crew member fell through an opening left by removed gratings. What primary safety management failures contributed to this incident?

  • Effective implementation of the Control of Work and Permit to Work Systems, combined with high situational awareness.
  • Inadequate communication between deck personnel, lack of situational awareness regarding SIMOPS, and absence of barriers or signage around the hazard. (correct)
  • The crew member disregarded the work instructions given.
  • The incident occurred during a non-routine task, which inherently carries higher risk.

A worker became entangled in a conveyor belt after it unexpectedly restarted during repair work. Which oversight directly led to this incident?

  • The worker knowingly bypassed safety protocols to expedite the repair.
  • The site supervisor was distracted and failed to complete the Permit to Work and isolate the conveyor line. (correct)
  • The site supervisor promptly completed the Permit to Work before the repair began.
  • The repair work was deemed low-risk, negating the need for a Permit to Work.

A crew member suffered a fractured finger while manually handling a metal plate on deck. What design flaw and procedural oversight contributed to the injury?

<p>The plate design did not allow for safe handling, and the available JSA was generic and not task-specific. (C)</p>
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A significant leak of LPG occurred at a refinery due to multiple failures. Which of the following represents a combination of factors that led to the incident?

<p>Unusually high pressure in the pipework, lack of discrepancy detection, and failure to take necessary measures. (A)</p>
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Flashcards

What is a Permit to Work (PTW)?

A formal process used to control, communicate, and coordinate activities, especially when potential hazards are present.

What are the causes of the 'Fall from Height' LTI?

A lack of awareness of simultaneous operations and inadequate deck communication

What caused the worker to be injured by the conveyor belt?

The site supervisor failed to implement company policy and procedure in respect of Permits to Work and isolation.

What injury occurred while handling metal plates?

A pinch injury to a crew member's finger while manually handling a metal plate.

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What caused the uncontrolled release of LPG?

The measures required to prevent incidents should be proportionate to the risks.

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Study Notes

Permit to Work and Isolation Incident

  • An electrician was installing fuses on a live 930V DC electrical system
  • Under-deck carousels had mechanical and electrical isolation as a safety measure for maintenance
  • Other critical vessel systems were powered by the same drive cabinet
  • Electrical isolation involved removing fuses for the carousel drive unit
  • Initially, the vessel was in port when the fuses were removed, and no other systems from the drive cabinet were powered
  • Breakers were isolated, and fuses removed to completely cut power to the drive cabinet
  • Fuses were left at the cabinet's bottom without tags, and the cabinet remained unlocked
  • Another electrician re-installed the fuses after maintenance
  • The electrician who re-installed the fuses believed the cabinet was isolated
  • A fuse insertion tool rated to 1000V was used to remove the protective mesh before the fuses were installed
  • An arc flash occurred, and the fuse blew when the second fuse was inserted
  • The electrician was not injured

Factors that contributed to the incident

  • No Permit To Work (PTW) was in place for activity control, communication, and coordination
  • The work team did not understand the company's required control levels for electrical work and isolations
  • Isolations were incorrectly applied
  • Vessel Standard Operating Procedures (SOP) did not account for long-term isolations
  • The SOP's should have included a safety requirement to protect multiple workers in the area
  • Security protocols for the electrical cabinet were not followed
  • The electrician did not lock and tag the cabinet after removing fuses
  • Toolbox Talk (TBT) regarding isolation requirements were not followed
  • The electrician re-installing the fuses failed to verify the drive cabinet's isolation before starting work
  • The electrician also failed to follow cabinet instructions and work instructions
  • Review procedures, work instructions, and risk assessments for Permit to Work and electrical isolations
  • Review Toolbox Talks to ensure they encompass all Permit to Work and isolation-related aspects
  • Verify system isolation BEFORE starting any work
  • Adhere to workplace instructions and warning signs

Fall from Height Incident

  • A Marine Safety Forum report detailed an incident where someone fell from the bridge deck to the deck below
  • Two teams of four crew members performed vessel superstructure maintenance
  • One team worked on the monkey island, the other on the bridge level gantry
  • The bridge level gantry team removed gratings and worked on the gantry's steel frame
  • The monkey island team moved to the bridge level after finishing their task
  • A crew member removed his safety harness
  • The crew member saw a paint drip and decided to address it and do a final check before break
  • Space constraints forced the crew member to walk backward without looking for hazards
  • A 3m fall occurred when the crew member stepped backwards through an opening left by a removed grating section
  • The grating was located on the boat deck
  • The MSF’s member reported an LTI

Causes for the fall

  • Control of Work and Permit to Work systems were not effectively implemented
  • There was inadequate situational awareness, risk perception, Simultaneous Operations (SIMOPS) awareness
  • The deck personnel in charge and the deck crew had inadequate communications
  • There weren't any barriers or signage present in the incident area
  • The removal of bridge gantry gratings created a fall hazard
  • Conduct more effective toolbox talks and pre-task risk assessments, with a focus on non-routine tasks
  • Apply a more thorough review of SIMOPS
  • During work planning, identify any combined operations and SIMOPS-related hazards
  • Determine whether SIMOPS can be avoided or tasks can be executed at different times
  • Assess the level of risk associated with SIMOPS
  • Evaluate whether planned control measures are adequate
  • Implement additional risk reduction measures and update risk assessments if planned controls are inadequate
  • Keep Incident records to prevent recurrence
  • Contribute to the Permit to Work and Control of Work process, and integrate any identified changes

UK HSE: Poor Control of Work Incident

  • An individual supervisor was sentenced for safety breaches
  • A worker became entangled in a conveyor belt, suffering serious hand and arm injuries

What happened

  • A worker started repairing a damaged conveyor belt
  • The conveyor belt started moving and his arm became entangled, causing muscle and tissue damage

Causes

  • The site supervisor was responsible for completing a Permit to Work and isolating the line, but failed to do so due to a distraction
  • The conveyor belt restarted during the repair work, leading to the employee's injury
  • The site supervisor did not implement company policy and procedures for Permits to Work and isolation
  • The inspector stated that the incident could have been easily avoided by doing correct control measures and safe work practices

Fracture during metal plate handling

  • While working on deck, a crew member suffered a pinch injury
  • The injury was to the right hand baby finger, resulting in a distal fracture and laceration
  • Sutures were required to close the finger's laceration

Causes

  • Heavy weather damaged deck plates
  • The injured person suffered a finger pinch injury between the plate and frame
  • An X-ray showed a distal fracture to the tip of the finger and the wound required stitches
  • The design of the plate had no considerations for safe manual handling
  • The plate installation had a permanent risk of finger entrapment
  • Risk assessments and toolbox talks were generic and not specific to the task
  • The JSA covered hot work only, and did not cover manual handling

Lessons Learned

  • Safety by Design: Modify plates with temporary handles to maintain finger safety
  • Utilize magnetic lifting handles
  • Take care with generic risk assessments
  • Modify them to suit the task, or use a dynamic risk assessment or toolbox talk for a full and thorough review of the task
  • Use the toolbox talk or JSA to define and understand areas of risk if the task is slow, uncomfortable, or inconvenient

UK HSE: Liquid Petroleum Gas (LPG) Leak

  • The operator of the UK’s largest oil refinery was fined for health and safety breaches
  • A leak of liquid petroleum gas (LPG) was discovered by a worker cycling home at the end of their shift

What happened

  • Around 15 tonnes of LPG was released through a valve near a roadway used by LPG road tankers visiting a refinery in Fawley, Hants, UK
  • The leak was undetected for around four hours before being discovered by an employee on his way home
  • It took a further hour to find the source of the leak and reset the valve via on-site emergency personnel

What went wrong

  • LPG was put through the pipe work at too high a pressure for the valve
  • There was no process to detect discrepancies in the flow in the pipe
  • The company failed to take necessary measures to prevent the major incident
  • The inspector said required prevention measures should be proportionate to the risks
  • Where companies handle large quantities of substances that can cause major incidents, such as LPG, they are required to have layers of protection in place to prevent incidents
  • A number of protection layers either failed or were not in place
  • Even though there was no fire or injury that occurred, there was potential for a high severity incident
  • The prosecution has been brought to highlight the importance of maintaining the layers of protection and preventing incidents </

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