Diving Bell Bailout Manifold Failure

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Questions and Answers

What was the immediate action taken after the bailout manifold failure was discovered?

  • Isolate the affected section and continue with unaffected operations
  • Notify the manufacturer and await further instructions
  • Immediately suspend diving operations and surface both bells (correct)
  • Continue diving operations with caution

What may uneven rubber boots on cylinders lead to?

  • Improved grip on surfaces
  • Even distribution of weight
  • Reduced cylinder pressure
  • Stress on one side of the cylinder (correct)

What should be the orientation of master link handles to ensure correct operation?

  • Facing outward away from the hook latch and lifeboat
  • Facing inboard towards the hook latch and lifeboat
  • Orientated to the sides (correct)
  • Facing upwards for easy access

What was the direct cause of the accident involving the lifting trunnion?

<p>The side forces experienced by the cover plate exceeded the screw's withstanding capacity (C)</p> Signup and view all the answers

What did the engineers notice about the water being flushed through the hose?

<p>The water had some yellow/brown liquid present (B)</p> Signup and view all the answers

Flashcards

Bailout Manifold Failure

Failure of a diving bell bailout manifold due to stress corrosion cracking and material ingress.

Lifeboat Release Failure

Master links disconnected due to handles facing inboard, impacting the hook safety latch.

Sheared Lifting Bolts

Cover plate of lifting trunnion fell off due to sheared screws, caused by side forces exceeding screw strength.

Hose Contamination Incident

A person felt ill after exposure to a hose containing residual Antifrogen (cooling agent) due to improper flushing and storage.

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Chemical Burns from Grout

Grouting dust mixed with water caused chemical burns due to a lack of hazard information on the Safety Data Sheet.

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Study Notes

Bailout Manifold Failure

  • A diving bell bailout manifold failed due to pressure while no divers were in the bell.
  • The bell was being prepared for diving, with the bell trunk isolated at 31msw and the system at 32msw.
  • A dive supervisor heard a gas rush, and a camera check revealed misting from a gas leak.
  • Four pieces of a failed nut were discovered from the bailout manifold assembly
  • Diving operations were suspended, and all bailouts were removed for inspection.
  • Uneven rubber boots on each cylinder likely caused stress on one side when moved.
  • The securing strap holding the bottles was loose.
  • The design of the bailout manifold was less robust compared to others.
  • Lateral force from inappropriate securing mechanisms likely caused stress corrosion cracking.
  • This led to material ingress and internal corrosion over time.
  • Existing bailout manifold assemblies were replaced with a robust version, and a reminder to ensure awareness maintenance tasks related to bailout alignment, integrity and boots, occurred
  • The nuts were made from copper alloy CW614N, susceptible to stress corrosion cracking and dezincification and are widely used in the industry.
  • A vessel was waiting on weather and was completing annual checks, including a lifeboat launch.
  • The unmanned launch led to the fore and aft master links disconnecting in an uncontrolled way while in the water.
  • There were no injuries, but the lifeboat was slightly damaged.
  • The lifeboat was lowered, the weight was taken, and the falls slacked.
  • The forward master link disconnected.
  • The crew in the rescue boat monitored the lifeboat.
  • As the rescue boat approached, the aft master link disconnected.
  • The lifeboat was tethered by forward and aft painters.
  • The forward painter disconnected after the forward master link hit the painter release system.
  • The lifeboat swung 180 degrees, the aft painter connected to the bitt released and the lifeboat drifted away.
  • The rescue boat and quayside crew recovered the lifeboat.
  • Incorrectly oriented master link handles faced inboard towards the hook latch and lifeboat.
  • Movement of the handles impacted and released the hook safety latch, releasing the hooks.
  • Action includes to replace master links with handles orientated to the sides.

Three Bolts Sheared on a Lifting Trunnion

  • After installing an offshore renewables Transition Piece (TP), the cover plate of the lifting trunnion was found fallen off on the hatch cover of the TP.
  • The three securing screws had sheared.
  • The cover plate weighed 44kg and fell approximately 0.5m.
  • Damage occurred to a survey beam and a GNSS positioning equipment antenna.
  • The antenna was fixed onboard; the survey lifting beam was replaced.
  • The method of verifying the suitability of the screws was incorrect.
  • It was assumed that sideway forces were introduced in the center of the lug cover, resulting in an inadequate securing method.
  • A permit to work was used, a toolbox talk was held, a Job hazard analysis was referenced, a Last-minute risk assessment was used, and the task plan was followed throughout installation.
  • Side forces exceeded the screw's capacity, likely due to human error, and the cover plates are to be welded to the lifting trunnions.

Hose Management and Chemicals

  • While filling a bucket from a hose, someone was adversely affected by the contents.
  • Two engineers were flushing non-potable water through a hose before filling a cooling water system.
  • One engineer started coughing and was escorted to the bridge, after which they recovered with rest and fresh air with no long-term effects sustained
  • The engineers noticed yellow/brown liquid, but it was assumed to be water.
  • The affected person was not wearing gloves.
  • The hose contained stagnant water and cooling medium liquid, having been coiled in a cupboard for nearly two years, which had previously been used to fill system with Antifrogen in Jul 2019 and was not properly flushed.
  • Old Hose was disposed of and two new hoses were prepared, one for cooling agent, one for non-potable water, and to avoid touching unknown substances.

Chemical Reaction

  • Post grouting operation for an offshore wind farm transition piece, a sub-contract grouting team cleaned equipment with high pressure water jets, resulting in of the team member receiving first degree burns to his knees and left calf in three places
  • Burns were healable and cured in the span of three weeks
  • A person with grouting dust on coveralls started working with a water jet, soaking their skin, causing a corrosive solution
  • The Safety Data Sheet lacked information on the hazard of grout dust mixing with water and becoming corrosive, leading to no risk mitigation.

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